The Cast Iron Jigsaw
Restoring the Camellia House at Wollaton Hall
Stuart Armitage
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| Figure 1: Interior of the restored Camellia House |
Rather forlorn and dogged by
vandalism, by 2004 the Camellia House at
Wollaton Hall, Nottinghamshire was closed
to the public. The once grand glasshouse had
sadly been fenced off, both to protect the public
from falling debris and glass, and to prevent
further damage to the structure.The glasshouse
was built in 1823 for the Willoughby family,
owners of Wollaton Hall, and was designed
especially to house the stunning camellia plants
they collected.
In plan, the building is laid out with four
quadrangles, each of which is covered by a
glazed pitched roof (see Figure 3). These roofs
drain into a gutter around their perimeter.
The walkways which separate and surround
each quadrangle are covered by barrel roofs
comprised of wrought iron panels which span
between the gutter positions. To convey the
water from the roofs into an underground
rainwater system, the gutters drain down
through the structural columns which support
them (see Figure 4).
In addition to using the columns as
downpipes, the builders had quite boldly
selected glazing bars with a very small section,
no doubt at the insistence of their clients, to
give maximum light within the Camellia House.
Two of the four perimeter walls of this
building are fully glazed with iron glazing bars
and a mixture of timber and iron doors. The
other two walls are constructed of brick faced
with render, and contain a number of recesses
for statues and benches. To the rear, where the
wall forms a retaining wall, there is a boiler
house, and at the bottom of a floor-well the remains of the boiler were found. This, we
believe, would have heated rainwater to provide
a hot and humid atmosphere throughout the
building as, at that time, it was not realised
that camellias are in fact quite hardy. A large
cistern was also uncovered during the works.
Hot air was circulated through an ingenious
arrangement of pipes, underground gullies and
vents, as well as through brick vaults beneath
the beds themselves. This must have required
a fairly sophisticated control system, allowing
the climate of the glasshouse to be carefully
managed.
However, as with many cast iron structures,
the ingenuity of its design was also its Achilles’
Heel. In particular, incorporating the rainwater
drainage system into the structural components
of the Camellia House was clever, but it also
seriously compromised the structure’s longevity.
Although the poor condition of the
building had been recognised before the
restoration work began, it soon became
apparent that the defects were much more
extensive than could have been foreseen at the
outset. This was mainly due to the enormous
build up of paints and fillers which had been
applied on an ad hoc basis over the years.
The project team included Purcell Miller
Tritton architects, who led the project, engineers
from The Morton Partnership, who advised
on the repairs, and Dorothea Restorations, the
contractor carrying out the works. The project
was part of a larger one which covered the
whole Wollaton Estate, and was run in parallel
with extensive repairs to the main hall under
the same project team.
The overall cost of the restoration was
approximately £1.1million, and the work lasted
just under two years. Thankfully, all of the
repair works were carried out with the camellias
in situ and without them suffering any damage.
Indeed by the time of the re-opening in 2007,
the camellias were already flowering.
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| Figure 2: The restored facade |
DISMANTLING, RECORDING AND INVESTIGATION
The process of renovation involved dismantling
the structure to allow proper fabric assessment,
repairs and sealing between components to prevent water ingress. This approach also
allowed the rainwater system to be properly
overhauled and repaired.
With approximately 900 components of
cast iron, wrought iron and glazing elements,
from the very start it was essential that an
appropriate logging and identification system be
established. A database was set up so that each
of the components could be individually tagged
with an identity number. This process allowed all
components to be tracked continuously, from the
time of removal from site right up to the time they
were returned and reinstated in the building.
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| Figure 3: Roofscape showing glazed pitched roofs with barrel roof in the foreground prior to restoration |
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This, however, was only one part of
the process to ensure that the building was
reconstructed to the exact same configuration as
before. Over a period of 180 years considerable
settlement had occurred to the building, and
general allowances had to be made for these
variations and for irregularities in the original
castings which were found to be far from
precise. This required meticulous surveying and
setting-out. A full dimensional survey of the structure
was therefore undertaken, both in the
horizontal and vertical planes, so that at key node points it would be possible to set the
building out exactly as it was found. This
meant that some gaps would remain between
components, but generally these discrepancies
would be distributed over the structure rather
than ending up with a shortfall at one position
or another or ending up with components that
simply could not be drawn together.
The system of data tagging also allowed
each component to be identified in terms of the
proposed repair types, and generally operated
as a useful tool in managing the process.
THE DEFECTS
Various masonry repairs to the rear wall,
which incorporated hidden lead downpipes,
as well as repairs to the boiler room and
adjacent stonework were necessary. The repairs
to the ironwork, however, were particularly
challenging and required a large amount of
careful decision-making to ensure that the most
appropriate type of repair was used in each
case. The vast number of components meant
that the decision-making process for repairs
needed to be clear, confident and rapid.
Once the components had been returned
to the workshop of Dorothea Restorations at
Whaley Bridge in Derbyshire, each was gathered
together according to type and then gritblasted
to reveal the true condition of the fabric
beneath the layers of rust and paint. Not only
were extensive additional defects discovered,
but also numerous historic repairs were found,
some of which were still sound (see Figure 5).
Generally, the components could be
categorised as being either small items of
decoration or related to the glazing elements,
or large elements relating to the main facades and structure. The large elements included 61
columns and many cast facade plates, some of
which were in the order of five metres long by
one metre deep.
It was clear that the idea of incorporating
rainwater drainage into the structure had been
fundamental to its design. For example, the
ribs which act as rafters between the glazed
panels and which also support the wrought
iron coverings to the walkways, all incorporated
a central rill to carry water from the adjacent
panels down into the gutters. The gutters
themselves are the spanning element between
the column positions and are carefully moulded
at the head of the columns so that the water
collected would then discharge down through
the column to the base and the underground
system.
Predictably, much of the decay was identified around the key fixing positions and
the positions where members were seated
together (see Figure 6). Often it was necessary
to make the repairs flush with the original
surface in order for the component to fit,
and indeed this type of repair posed certain
difficulties in itself. The key defect positions
were at the bottom of the ribs and on the
columns themselves. There were also quite
extensive fractures in the cast gutters, and
general movement of the building had caused
fractures within the large plates associated with
the facade.
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| Figure 5: Earlier plate repair |
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| Figure 4: Internal columns and gutter beams. The hollow columns also serve as downpipes |
Figure 6: Typical corrosion at joint of cast iron members |
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| Figure 8: Column ends showing off-centre cores and lining materials from earlier repairs |
| Figure 7: Fractured column |
Damage to the columns was primarily the
result of corrosion and frost action which had
caused fractures to occur, often with splits from
top to bottom (see Figure 7). Several factors
were responsible. Firstly, the rainwater conduits
within were only 38mm in diameter and were
easily blocked by falling debris. Secondly, in
many cases the core appears to have floated
when they were first cast, resulting in a thinner
wall section on one side of the column. This was
made worse by the deeply recessed moulding
to the external face of the column, which in
some cases meant that there was only 6mm or
so of material between the recess on the outer
face of the column and the edge of its hollow
core. In a number of cases, historic attempts
to line the columns with plastic or lead pipes
had in fact made the situation worse, either
because rainwater from the top found its way
between the sleeve and the iron, or because
condensation had accumulated between the two
materials, causing further decay (see Figure 8).
Within the smaller components the quality
of the original castings was reasonable. Due
to their size, the distortions in them were
proportionally fairly small. However, extensive
areas of the larger components were pitted with
holes and in fairly poor condition and many
suffered from a significant degree of warp across
their full surface area.
Problems like these often go unrecognised
until the really detailed stage of a project when
every single component is studied, and this
was quite a painstaking and lengthy process.
It was, however, significant that by working
closely with the contractors in their workshop,
this process was made very much easier and a
principle was established for dealing with each
type of situation which could then be repeated
as necessary.
A further problem was presented by
the high iron content of the castings: within
hours of grit-blasting a component the orange
discolouration of rust was beginning to develop.
This meant that, before the final painting
process, each component had to be lightly
blasted once again.
REPAIRING THE IRONWORK
In terms of the rationale for the repairs, the
key to this type of structure relates to its
overall appearance. It was realised very early
on that, on a local scale, the repairs needed to
be functional and robust due to the structural
role of many of the components. However,
the beauty of the structure is primarily
appreciated when the building is viewed in
its entirety, rather than in detail, so there was
little requirement for invisible repairs. Indeed
it is doubtful whether repairs could have been
achieved which would have been both truly
effective and invisible.
In terms of the repairs, there was a
proportion of re-casting required, and this
particularly applied to the columns which
formed the downpipes. As several of the
columns needed to be cast, it was most efficient
to make a new timber mould based on one of
the original columns and use this for the recasts.
To solve the problem of the floating core,
small sacrificial pins were introduced between
the core mould and the outer mould to hold
the core in place and ensure a consistent wall
thickness around it. The pins then melted into
the casting.
Other repairs included limited welding and
stitch repairs between non-structural elements,
particularly to the large facade plates, and some
bolted structural repairs, particularly related
to the bottom of the roofing ribs. For aesthetic
reasons, the number of large plated repairs
that would be visible externally was kept to a
minimum.
Where the cast ribs were found to be
rotten at the lower end, the metal was cut back
to sound material and new ends were cast
and then secured by dowels to the original.
This process was carried out by drilling the new casting then tapping this hole so that a
threaded pin could be used to secure the new
and existing sections together. The dowel was
resin fixed into the existing casting, and the
joint notched and welded.
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| Figure 9: Floor vents of heating and humidification
system |
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The final element was the repair of the
floor beams. The floor system incorporated the
drains and the humidifiers. It consisted of deep
trenches running beneath all of the paths to allow water collected from the roof to be heated
by circulatory pipes. Bronze grilles in the floor
above then emitted warm, moist air back into
the Camellia House (see Figure 9). The slabs
over the top of these deep drainage gullies,
which were up to 1.5m wide, were supported
on T-section cast iron joists, with the vertical
web members becoming deeper towards the
centre, and the joists terminated in a heavy
block at each end. There were complicated joist
intersections beneath crossing paths including
cast dovetail joints.
Removal of the floor slab was possible only
after the building had been dismantled since
most of the perimeter paving was inaccessible
beneath the cast walls of the Camellia House.
Once lifted it was obvious that many of the
joists were rotten. The rot particularly occurred
at the position where the beam spanned over
the bearing position and at the face of the
drainage channel. These members clearly had to
be replaced, and either stainless steel angles or
new cast iron joists were used. There were other
members which appeared to be sound, but on
close inspection minor fractures could be seen.
Although small, these were potentially sufficient
for the members to fail.
At that stage in the works, we talked in
some depth about options for investigations,
even fleetingly considering the idea of
x-raying the members in order to reveal minor
fractures. However, it was decided that the most
pragmatic approach was to test the beams on
site. For this a rather rudimentary approach was
taken; each of the beams was simply propped
on bricks at either end so that they spanned
freely. Then, in turn, each of the beams was
stood on by the engineer or a contractor. Some
failed immediately and had to be replaced,
while others were perfectly satisfactory and
could be reinstated.
Interestingly, looking at those beams that
had failed, there probably was no other way of
readily determining whether or not these beams
were deficient and fractured. When the fracture
point of a beam that failed was inspected, it was
usually possible to see that rust ingress affecting
the cross-section had left only a very small
thickness of solid grey cast iron core between
the rust margins.
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| Figure 10: Re-erecting the repaired ribs and gutters |
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| Figure 11: Glazed quadrangle |
Figure 12: Glazing detail |
In a sense, the way this particular element
was dealt with illustrates the overall approach.
Glasshouses are elegant in their form when
considered as a whole, but ultimately they are
engineered structures. This rather direct and
simple approach therefore seems completely
appropriate and in the spirit of the type of
building being repaired.
Once all the repairs had been carried out,
the members were grit-blasted again and then
primed. It was decided that the members would
be fully re-painted before being returned to site
and then given just a final touch-up to cover
any damage which had occurred during transit
or re-erection.
The ground and below-ground drainage
gullies were repaired and a new outlet was
constructed to remove water from the system.
Since the full mechanism of the heating and
humidification system, including its boiler,
was not being reinstated, it was not feasible to
restore all components of the drainage system.
However, we did ensure that the collected
rainwater could be removed from the network
of trenches beneath the floor. Fortunately, to
the perimeter of the Camellia House lawn there
is a retaining structure forming a ha-ha and the
water could be discharged beyond this point.
REASSEMBLY
When the members were finally ready for
re-erection, the structure began to take shape
on site in July 2006 (see Figure 10). Once
re-erected, and without fillers, inserts and
other material, it was quite obvious that the
alignment of some of the castings was far from
perfect. It was therefore once again necessary
to use a certain amount of filler, particularly at
junctions between components, to make the
structure waterproof.
The process of glazing was then carried out
with the help of an internal scaffold below and
flying walkways above, as the structure of the
roof around the panels was not strong enough
to allow safe access from above. The handmade
glass provided beautiful texture and reflection of
light within the structure (see Figure 11).
A new lightweight over-roof structure
comprising steel frames and ETFE (Ethylene
Tetra Fluoro Ethylene) cushions was then
installed to offer some protection against
vandalism to the glazed panels. The frame
structure was supported from small adjustable
legs (visible in
Figure 1) which sit in each of the gutters.
Finally, the whole building was checked for
watertightness, and the paintwork touched-up
to successfully complete the project.
Looking back, the key to the success of this
project lay in the close working relationship
between the engineer and the contractors, the
very much hands-on approach at the workshop,
and a real sense of wanting to get the structure
repaired correctly and in a robust manner.
There was a feeling that because the building
was completely dismantled, this would be
perhaps the only opportunity for another 150
years to undertake such extensive repairs so
they simply had to be right.
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This
article is reproduced from The Building Conservation Directory, 2008
Author
STUART ARMITAGE, an engineer with
The Morton Partnership, was the
structural engineer responsible for the repair
of the Camellia House at Wollaton Hall.
The Camellia House is owned by Nottingham
City Council, and is open on selected days to the
public, along with the park and hall.
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information
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